Early U.S. Navy Afterburner Development Efforts
Part 3e: McDonnell Aircraft Corporation – Continued Development and Flight Test
by Paul J. Christiansen
Published 2 Jul 2026
| Part 1: Ryan Aeronautical | Part 2a: Solar Aircraft: Early Design and Development |
| Part 2b: Solar Aircraft: Production Design and Development | Part 2c: Solar Aircraft: Production Testing and Continued Development |
| Part 2d: Solar Aircraft: Production Testing and Continued Development | Part 2e: Solar Aircraft: Final Testing and Program End |
| Part 3a: McDonnell Aircraft: Initial Proposal and Development | Part 3b: McDonnell Aircraft: Continued Development |
| Part 3c: McDonnell Aircraft: Continued Development | Part 3d: McDonnell Aircraft: Continued Development and Flight Test |
| Part 3e: McDonnell Aircraft: Continued Development and Flight Test | Part 3f: McDonnell Aircraft: (in process) |
| Part 4: Westinghouse Aviation Gas Turbine Division (in process) | Part 4: Westinghouse Aviation Gas Turbine Division (in process) |
McDonnell Aircraft, St. Louis, Missouri
23 October 1949: Muroc Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1357.
Further background on the intent of JA‑34‑MD‑15 AB tests in the XF‑88A was given. The primary objective was to determine the best fuel‑air ratio for maximum thrust augmentation at all altitudes. The original fuel control was to have a fixed nozzle area for wet operation and allow a by‑pass motor valve, regulated by the TOT, to maintain balanced‑cycle operation throughout the range of altitudes. This approach had proved to be unsatisfactory by itself since the motor by‑pass valve had sufficient capacity only for regulation over a range of 3,000 – 4,000 ft of altitude for one fixed nozzle area.
As a result, it was deemed necessary to have, for test purposes, a method for the pilot to vary the nozzle area. Three fuel‑air ratios were tested by means of flow adjustment on the AB fuel control valve and flights to various airspeeds and altitudes. During the flights, the nozzle area was pilot‑adjusted to maintain balance‑cycle operation. This was the TOT limit at 12,500 rpm with the AB wet. To maintain the constant fuel‑air ratio the motor valve was disconnected from the system. The result was that all control of the fuel flow for balance‑cycle was through the nozzle area adjustment.
Of the three ratios tested, 0.044 proved the best ratio, providing the best augmentation. This was determined by the attainment of the highest maximum airplane speed, both ABs wet and using a fuel‑air ratio versus nozzle area plot for balanced‑cycle operation. This determination method was chosen over the use of compressor differential versus AB fuel flow since a change in nozzle area reflected any change in the compressor differential and consequent fuel flow. The plot had also shown that there was no indication of a peak efficiency having been obtained with the fuel‑air ratios tested with this JA‑34‑MD‑15 burner. Such a peak would have manifested itself in a drop‑off nozzle area required for an increase in the fuel‑air ratio. Speed variation had had little effect on the nozzle area required. While insufficient fuel‑air ratios were obtained to definitely establish a curve, the general trend of the variation was indicated.
Testing of the JA‑34‑MD‑15 model indicated that the best efficiency could not be obtained by having the outer fuel injection nozzles spraying directly toward the burner center as the changing flow patterns through the burner were directing fuel away from the flame holders. To improve things, the outer burner ring fuel injection nozzles were changed so that fuel was now injected away from the burner center by lengthening each nozzle and bending it 180°. The outer flame holder slope was also changed slightly. The new burner was designated the JA‑34‑MD‑16.
Since the new burners would obtain maximum efficiency at a lower fuel‑air ratio than the JA‑34‑MD‑15 model, a new testing technique was required and would be applied. The AB fuel by‑pass motor valve would be made operative, regulated by limiting the TOT. At a selected altitude, the pilot would select a series of nozzle areas allowing the motor valve to regulate the fuel flow for red line temperature and the consequent fuel‑air ratio. The tests would be repeated for two or three altitudes. The fuel‑air ratio data collected from the curves for each altitude would allow the fuel supply curve slope to be set.
| AB Operating Times Summary for the Entire Test Series, 1 September to 12 October | |
|---|---|
| Total Flights with Afterburning | 26 |
| Total Single AB Take‑offs | 25 |
| Total Dual AB Take‑offs | 1 |
| Total AB Flight Time | 3.28 hr |
| Total AB Time Including Ground Operation | 4.65 hr |
The JA‑34‑MD‑16 ABs were installed and the engines (WE020017 and WE020103) were calibrated with the new ABs. WE020103 with AB No. 4 was installed as the L/H engine. WE020017 while No. 5 was installed as the R/H engine. Additional fiberglass insulation was installed under the stainless steel heat shield to provide more thermal protection during AB operation. Ground runs were made with the fuel flow schedule set with the pressure‑operated valve to give a fuel‑air ratio from 0.035 to 0.040.
30 October 1949: Muroc Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1436.
Low altitude testing began with the fuel flow set to provide a fuel‑air ratio considered very nearly optimum for low altitudes and high speed operation as had been determined from test cell data. Two flights were dedicated to check the nozzle positioning apparatus functioning and the development of hot spots. Initially it was found impossible to obtain red line TOT on the L/H AB due to intermittent nozzle control. Two observed dark spots behind the flame holder struts were eliminated by pinching the outer ring fuel nozzles adjacent to the struts. Considerable difficulty was encountered in flights 41 and 42 in nozzle area adjustment and during flight 41 full open nozzle area could not be attained; adjustments were made by rerouting the tele‑flex cables to eliminate binding. This was only partially effective and problems were experienced on the next flight on the L/H AB. Data was obtained at 0.8 Mach with both ABs wet at 10,000 feet. A dual AB run was made at 10,000 ft during flight 43. During the take‑off of flight 43 with both ABs wet, the pilot had difficulty in keeping the TOT within 20°C of the red lines. Due to differences indicated in the cockpit between the L/H and R/H AB areas, it was suspected that the R/H area shown on the cockpit indicator was not accurate. The instrumentation was to be inspected.
| AB Operating Times Summary for the Entire Test Series, 1 September to 12 October | |
|---|---|
| 46‑526 | |
| Total Flights During which ABs were Used | 29 |
| Total Take‑offs with One AB Operating | 25 |
| Total Take‑offs with Both ABs Operating | 2 |
| Total AB Flight Time | 3.58 hr |
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| JA-34-MD-15 Afterburner | JA-34-MD-16 Afterburner |
Additional data on the design difference between the ‑15 and ‑16 models was given. The combustor section had been redesigned to eliminate the faired‑over wall step flame holder of the ‑15 and now incorporated instead an optimum divider step flame holder diffuser in the design. Also, the radially inward injection of fuel from the outer burner ring was changed to provide radially outward fuel injection by use of hook type nozzles. It was expected the new combustor design would give longer nozzle life due to cooler outer strata of gases. The fuel injection nozzle change was expected to result in improved performance and ignition characteristics.
5 November 1949: The Bureau of Aeronautics Resident Representative (BARR) reported that McD had requested an increase in the rejection to overhaul limit for AB operating time; as then established in Engine Bulletin No. 37; from two (2) to three (3) hours. The change would be consistent with the recent increase in all condition time and Military time from 50 to 150 and 5 to 10 hours respectively. Experience had shown that in no case was a deficiency found in an engine after two hours of AB time that would not have been found by inspecting the engine after every two hours of Military time. If the extension was granted for total AB time, sufficient time was available on the current engines to complete the current AB test program on the F2H‑1. If not granted, three additional engines would be required. The current spare engine WE022017 had only 25 minutes of allowable AB time remaining.
7 November 1949: Muroc Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1438. On flight 526‑45 the AB fuel by‑pass valves were made operative and the program to determine the optimum fuel‑gas ratios begun. This first flight in the program went to 15,000 ft with plans to vary the nozzle area and allow the motor valve to adjust the fuel flow to balanced cycle. Unfortunately, no data were obtained due to the inability to properly adjust the L/H nozzle area and the improper ignition and burning on the R/H engine.
Post flight ground runs showed that proper burning could not be maintained using the recommended 0.75:1 fuel ratio between the inner/outer rings when used in the current AB configuration. Also, it was discovered that the L/H nozzle actuation control relays were intermittent, preventing proper nozzle adjustment. Actions taken were to change the fuel manifold ratio to 1:1 and the replacing the relay box. The flight plan was to be repeated on flight 526‑46 but this flight suffered an overheat warning on the L/H engine. The flight was aborted and a single engine cross wind landing was attempted. On touch down, the left‑hand main gear leg failed and a minor crash occurred. The pilot was uninjured. The airframe was to be returned by truck from Muroc to McD’s company facilities in St. Louis for repair.
9 November 1949: McDonnell Accident Report, Model F2H‑1 Airplane, BuNo 122530, Report 1448. Flight 530‑187, on 26 October 1949, was terminated early after the pilot experienced symptoms of anoxia at 25,000 ft. The mission had been to make an early evaluation of the F2H‑1 airplane with McD JA‑34‑MD‑15 ABs installed. During the landing, the pilot flared too high. Rapid throttle advancement to the Normal position did nothing to reduce the sharp and rapid decent that had developed. The initial impact was on the main gears and a large bounce resulted. The second impact was primarily on the right main gear and after rolling to a stop the right tire was found to be flat. Several minutes later the left main gear tire was found to also be flat. Minor other damage was found but was too small to be photographed.
14 November 1949: The Navy Bureau of Aeronautics (BuAer) authorized the AB time limit on the three specific engines being used in the AB program to be raised from two to three hours. A Class B inspection was required on an engine after it accumulated two hours of AB operation. The BARR was to advise BuAer of the serial numbers on the engines affected.
16 November 1949: A request from McD for specified quantities five different type flight test instruments for the AB testing program was forwarded by BuAer to its Flight Test Division at Patuxent River. This informed McD that the instruments were to be returned to Pax River at the conclusion of the tests.
18 November 1949: Contract NOa(s)‑9768, Model F2H‑2 Airplanes – Proposal for Afterburner Installations, Report 892A‑31A.
McD responded to a request from BuAer for a price and a delivery proposal for the installation of McD short ABs in four (4) F2H‑2 airplanes. Discussion included McD’s observation that the development of automatic controls for ABs had not kept pace with AB development and a major effort was needed to advance controls development in order to have automatic controls available for service test. The current process of controlling the temperatures using electric switches was adequate for experimental test flight operation but was not considered safe for service test purposes.
The projected price for development and ground tests, F2H modifications, flight tests, liaison and service qualification tests was $624,100.00. Since the Navy wished there to be no increase in the contract NOa(s)‑9022, McD suggested a postponement of price redetermination of that contract and consideration be made to issuing a “no price increase amendment” to Contract NOa(s)‑9768. The proposal superseded all prior proposals and was based on the acceptance and concurrent performance of the work covered in McD’s letter (actually not received until 22 December 1949, and not found).
Deliverables would be two variable‑nozzle ABs of McD design essentially similar to those installed in F2H‑1 BuNo 122530, two spare ABs and two spare sets of AB controls packed for domestic shipment FOB McD’s plant. Delivery of all items would be four (4) months after receipt of authorization to proceed.
23 November 1949: McDonnell Aircraft Corporation, Accident Report, XF‑88A Airplane 46‑526, Flight 526‑45, Contract W33‑038‑sc‑14582. The L/H engine was cut off immediately after take‑off due to an overheat warning light. Even after cutoff, the warning light remained lit and was blinking. When the gear was lowered for a single engine landing, the L/H landing gear did not indicate down and locked and was recycled, the second try obtaining a down and locked condition indication. Altitude and speed were lost during the landing gear cycling. The aircraft was beginning to settle so the landing gear retraction was started for a go around attempt. Altitude was being lost so rapidly that the landing gear lever was moved to the down position again and the base turn discontinued. A cross‑wind landing on the lake was attempted. The airplane stalled 30 ft above the ground, flaps up, gross weight approximately 19,300 lb and a cross wind of 17.5 kts.
The main gear and tail skid contacted the ground. The left main gear collapsed and cleared the airplane after punching a hole in the underside of the left wing. The airplane then skidded 5,000 ft on the left wing tip, rolling on the right gear and nose wheel. Damage was confined to the left main gear, left wing, right wing gear attachment, L/H engine exhaust shroud, and the tail section. Inspection of the overheat detector system revealed that one bulb had been struck when installing the L/H afterburner, shorting the bulb internally. The light was still on when power was applied when inspected; moving the bulb slightly caused the light to go out.
28 November 1949: Installation and Evaluation of Afterburner in F2H‑1 Airplane under Contract NOa(s)‑9022, Progress Report for Period 16 August through 15 October 1949. The ABs installed in the F2H‑1 were JA34‑MD‑15 models. During the period, the primary flight test objective was F2H‑1 operational and performance characteristic investigation and improvement. The first flight test series was made to determine the optimum fuel flow and nozzle area for good AB performance over a range of altitudes and at airspeeds conducive to high rates of climb. Additionally, the initial flights were to familiarize the pilot with the AB installation and its controls as well as to adjust the engine governor for variable nozzle and AB operation.
Subsequently, short periods of AB wet operation in level flight were made at several altitudes up to 35,000 ft with approximately a 0.035 fuel/air ratio. Ignition was good up to 25,000 ft but above that altitude some partial ignition was obtained. Satisfactory ignition up to 35,000 ft could be obtained with proper piloting technique. The AB operation was quite sensitive above 25,000 ft to nozzle area variations and changes in transient conditions. One flight was made with both ABs wet from take‑off in a climb to 40,000 feet. Both ABs operated satisfactorily up to 31,000 ft. At that altitude the R/H AB blew out due to a sudden change in nozzle area. The L/H AB was turned off at 38,000 feet. A second climb was attempted to 40,000 ft with both ABs wet. The L/H AB was satisfactory up to 40,000 ft but the R/H AB blew out at 34,000 feet. The cause of this blowout had not yet been determined, but was thought to be related to a combination of rapidly changing, transient conditions and the necessity for close manual control of the nozzle area. The limitations of the current semi‑automatic control were obvious and an investigation was initiated with the objective of a control system able to provide complete fully automatic AB control. The next test period would focus on investigation and improvement of operation at higher altitudes. As of 15 October 1949, the L/H AB had accumulated 24.7 hr of engine time, 1.46 hr of which were AB wet. The R/H AB had 20.16 and 0.54 hr respectively.
Other static ground testing had continued at Westinghouse in Lester, Pennsylvania during the period. The AB model was designated the JA34‑MD‑16. Test results with a modified injection system had revealed that a variation in the fuel injection orifice position with respect to the flameholder had a large effect on performance. An optimum fuel injection orifice location was determined from tests. This modification gave a considerable improvement in AB ignitability, combustion stability and combustion efficiency. The fuel required for ignition was only 50% of that required for maximum (engine) thrust at static sea level conditions. The reduced fuel flow for ignition, improved performance over a range of fuel gas ratios and the higher combustion efficiency of the new model were expected to substantially improve the high altitude performance.
High temperature oxide gradients on the JA34‑MD‑15 AB nozzle had shown that the nozzle temperature was not uniform around the periphery during low fuel flow and high altitude AB operation. The cooler spot was in a position opposite the fuel manifold inlet and indicated the ‑15 had partial fuel vaporization within the manifolds. This could result in excessive heating of the AB fuel. It was possible that this factor contributed to combustion instability at high altitude. In the ‑16 model; heat transfer from the diffuser wall to the outer manifold was eliminated by supporting the manifold away from the wall and wrapping with asbestos insulation. The inner manifold was already mounted away from the wall in previous designs and was also wrapped with asbestos insulation. The new official designation for the improved model was the “M. A. C. Short Afterburner, Model JA34‑MD‑16”.
5 January 1950: Weekly Summary Flight Report Week Ending 1 January 1950, Report 1511.
Data was collected related to an investigation into the possible thrust increase at altitude if variable area nozzles were installed on Westinghouse J34 engines. (Just the engine nozzle, not AB related). The TOT was measured at altitudes up to 40,000 ft and at Mach numbers from 0.6 to 0.8 in order to determine the range of flight conditions under which it was possible to obtain TOT red‑line temperature using the present fixed area nozzles. The results were not yet available to report.
A climb to 40,000 ft was made with the entry speed raised from 0.70 Mach to 0.75 Mach. This was to determine if the improved airspeed would afford sufficient improvement in AB thrust to provide an increase in excess power and consequently in rate of climb. Since the new procedure also eliminated the previously used zoom at the end of the climb, the resulting data could not be directly compared to the previous climb data results. Also, the airplane gross weight was significantly different. It was going to be necessary to await completion of the reduction of all test data to standard conditions and to a common gross weight.
Operationally, the AB and engine operation was smooth throughout the climb. The sensitivity of the AB nozzle controls had been increased and this had apparently produced the desired effect as no appreciable TOT hunting had been evident. The TOT on the R/H engine had been stabilized but was 30°C below redline. Above 24,000 ft, the temperature on the L/H engine fell off slowly until at 40,000 ft it was approximately 100°C below redline. This indicated the minimum nozzle area was slightly greater than desirable for the flight condition. The rpm on both engines was steady and no excessive speeds were encountered.
13 January 1950: Justification for a Contract Amendment Negotiation. This amendment was to be put in place to implement McD’s suggestion to put their ABs on an F2H‑2 and do limited testing. If approved, it would be Amendment 19 to Contract NOa(s) 9768.
a. “Install in one F2H‑2 airplane a (crossed out and “two” written in) M.A.C. short afterburners (JA34‑MD‑16) with a fully automatic control system and conduct approximately 4 hours flight testing, in accordance with enclosure (1) and enclosure (A) thereto.
b. “Supply two (2) spare afterburners and two (2) spare sets of afterburner controls packed for domestic shipment f.o.b. contractor’s plant.” The $175,925.00 price was crossed out and “No Increase in Contract Price” written instead. The justification given was: “To provide an F2H‑2 airplane equipped with a MAC short afterburner with a fully automatic control system for flight evaluation of the afterburner, and for early investigation of the interceptor problems with an actual flight article.”
19 January 1950: Interim Summary Progress Report on Afterburner Tests, Report 1507. The report covered F2H‑1 flight tests when equipped with JA34‑MD (model not specified) up to 31 December 1949. It also included comparative analysis of the AB equipped airplane with a standard F2H‑1 not so equipped. At sea level, a 19,600 feet per minute rate of climb of was obtained as compared to 9,600 feet per minute obtained from a standard F2H‑1. At 40,000 ft, the rate of climb was 3,500 feet per minute compared to 1,800 feet per minute. The time to climb from sea level to 40,000 ft, corrected for standard conditions, was 4.4 minutes compared to the standard F2H‑1’s 8.6 minutes. The best of the actual climbs was accomplished by starting at a climbing speed at 2,000 feet and reaching 40,000 ft in 3.7 minutes. High speed with ABs was 23 kts higher than the standard F2H‑1 with J34‑WE‑22 engines and 15 kts higher than the airplane with the J34‑WE‑34 engines. The climbs were made with an interim automatic control that operated successfully up to the point where abnormal engine behavior occurred. This was suspected to be the cause of the compressor stalling experienced on AB shutdowns. The AB had been ignited and operated for a short time at 44,000 ft and operated throughout a Mach number range from 0.4 to 0.83 at 40,000 ft. This indicated that the combustion characteristics of the AB were satisfactory at altitudes in excess of the engine and governor operating limits. The fact that the measured performance was seen to be substantially equal to that calculated indicated the AB had a thrust augmentation almost up to that anticipated. Further improvements outlined in Enclosure (A) (not found) were fully expected to result in sufficient thrust augmentation to equal or exceed the performance estimated and also result in an AB of substantially increased service life. In view of the favorable results determined to date, McD requested that additional engines be assigned to carry on this flight test program. A written note attached says a final firm estimate of seven (7) engines was needed and a memorandum request was in progress. The Maintenance Division was requested to coordinate the diversion of the additional engines should the request be accepted. An undated second note says the memo was received and the seven engines had been provided. A third note dated 28 February 1950 says the Maintenance Division could not support a “carte blanche” approach to supporting the project. When a final firm estimate of the requirements was forthcoming in a memorandum from the Piloted Aircraft Division, a decision could be made as to the Maintenance Division’s ability to support the tests. A further concurrence with the latter note stated that the Maintenance Division could not provide blanket support for experimental programs. When the Power Plant Division and Aircraft Division determined the number of engines required for the program, the Maintenance Division could evaluate engine availability. (It is not possible to determine if the 7 engines were made available, but in March McD said they could complete their tests with the current engines on hand.)
12 February 1950: Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1568. After flight 526‑97 of the first XF‑88 serial 46‑525, the airframe was put in protracted work status for installation of McD short ABs and wing root fuel cells.
22 March 1950: BuAer asked McD to extend the tests work on the F2H‑1 being used for the AB testing to include installing variable nozzles of the engines and report the test results in the weekly summary reports. This was to be done at no increase in the contract price.
31 March 1950: McD reported the variable nozzle tests could be completed with the remainder of the Military time (4 hr) on the two engines then assigned to the AB tests, serials WE022096 and WE022121.
2 April 1950: Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1636. Prior to flight, in addition to airframe strengthening and additional fuel tank storage installation in the wing roots (in lieu of the fire extinguisher system in that space), the AB fuel system had automatic hot streak ignition and constant proportioner for inner and outer fuel rings added. All damage from the crash was repaired and McD JA34‑MD‑16B ABs were installed. The AB controls were modified to provide an emergency system that caused the nozzle to go full open during AB operation or full closed during non‑afterburner operation. Limited inverted flight capability was added by modifying the oil tanks with swivel pickups. On the XF‑88A, functional checks were performed and found to be generally satisfactory during climbs to 2,000 ft and level flight at 10,800 ft. A slight fluctuation in the TOT during a single AB climb from 15,000 to 30,000 ft was noted. The hot streak ignition was also checked and found to be satisfactory. Flights 526‑47 to 526‑52 were performed bringing the total flight time on the airframe to 36.09 hours.
| Total Flights where ABs Were Used | 38 |
| Take‑offs with One AB Operating | 27 |
| Take‑offs with Both ABs Operating | 11 |
| Total AB Time | 4.1 hrs |
It was thought a change in sensitivity on the amplifier controlling the variable nozzle would correct the TOT fluctuation issue.
9 April 1950: Weekly Summary Progress Report of XF‑88 & XF‑88A Report No. 1637. Further checks on the AB were performed on flights 526‑53 and 526‑54. These included two AB take‑offs, a climb from 15,000 to 30,000 ft (R/H AB wet only), automatic hot streak starts at 30,000 ft and a check of the manual nozzle control at high indicated airspeeds. All checks were generally satisfactory. Total airframe time after the two flights was now 38.34 hrs.
| Total Flights Where ABs were Used | 40 |
| Take‑offs with One AB Operating | 27 |
| Take‑offs with Both ABs Operating | 13 |
| Total AB Time | 4.4 hrs |
For the climb, the R/H AB was ignited at 0.5 Mach at 15,000 ft and the airframe accelerated to 0.75 Mach at which speed a climb was made to 30,000 ft. Automatic hot streak starts were made at 0.75, 0.80 and 0.85 Mach at 30,000 ft. Only partial light‑off was obtained at 0.75 Mach, but both the 0.80 and 0.85 Mach light‑offs were fully successful. The manual control on the nozzle was checked to be sure the variable nozzle actuators were powerful enough to close the nozzles at high exhaust velocities. The nozzles were opened and closed manually and the TOT returned to within 10°C of its former setting. This indicated the nozzle actuators were satisfactory at high air speeds. No quantitative data was collected during these functional checks.
A. The original estimate of 7 J34‑WE‑34 engines was based upon 2 engines for McD test stand use and probable NACA testing, plus 5 engines for flight tests. The latter number established by “ratioing” engines required to flight hours for present and proposed programs. No provisions were made for testing at Westinghouse since the assumption was made that all Westinghouse testing would be conducted with their test house engines as was previously done. (Note: Interestingly, the author had found no such mention of such in house engine usage in any BuAer or Westinghouse correspondence during his research for his book on J34 development.)
B. A second estimate of the total number of engines required was based on past engine failure experiences as follows:a. Engine times logged on each engine.
b. Since the times logged on the satisfactory engines generally exceeded the average of those logged on rejected engines, the estimate should not include the two remaining engines in the airplane. Those two engines would be used to conduct the authorized variable nozzle program.
Engine Serial No. All Conditions Military Power Afterburning WE022017 67.8 10.9 2.3 WE022044 16.4 3.1 0.5 WE022049 51.7 7.4 1.3 WE022117 24.2 3.3 0.5 WE022018* 10.1 0.4 None Engine Times for Engines Currently Installed WE022096 51.0 5.5 1.3 WE022121 43.4 4.9 1.5 *Not used in AB program as a 10 hr inspection had revealed a foreign object had passed through the engine cutting up the turbine area.
c. Experience with the AB program showed that only approximately one half of the engine time would be accumulated during flight. Assuming 35 hours of flight time for an extended AB program, four engines plus one engine for contingencies or five engines total would be required.
d. An additional two engines would still be required for McD test stand and NACA testing.